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橡塑技术与装备
HINA R&P TECHNOLOGY AND EQUIPMENT
5 成品性能
采用以上三个方案分别硫化成品胎送厂内里程实
验,结果见表 7,可以看出,方案三减少 1 min 硫化
时间的轮胎高速、耐久性能均满足标准。
表 7 成品胎性能对比
项目 方案一 方案二 方案三
3 130 3 356 3 446
耐久性能 /min
胎肩掉块 胎肩掉块 胎肩掉块
260 260 260
高速性能 /min
图 8 胎圈部位温度曲线 无损 无损 无损
6 结语
通过发泡测温结果表明,冬季低温胎胚相对夏季
硫化时间增加 30 s,高导热胶囊相对普通胶囊减少 30
s 硫化时间,在消泡位置胶囊厚度每增加 1 mm 硫化时
间增加 1 min。高低压管路串联增加排凝罐可有效减
少管路内冷凝水解决内里欠硫这个一直存在的问题。
根据以上结果工厂内平均硫化时间可减少 30 s,
按照平均单胎 9.5 kg,平均硫化时间 13 min,吨胎蒸
图 9 轮胎内部内衬温度
汽消耗 1.7 t,年产 800 万条,蒸汽每吨 280 元计算,
由以上图、表可知方案三各点温度均最高,通过 每年可减少蒸汽用量 4 969 t,降本 139 万元。
发泡实验方案三可以减少 1 min 硫化时间。
Reason analysis and measures for reducing time and improving
efficiency in tire vulcanization
Ren Qiaowei, Tan Miao, Li Xiaolin, Dang Fei, Du Fan
(Shaanxi Yanchang Petroleum (Group) Rubber Co. LTD., Xianyang 712000, Shaanxi, China)
Abstract: This article investigates the impact of tire blank temperature, capsule thickness, thermal
conductivity, and thermal pipelines on vulcanization time. In winter, the vulcanization time of tire blanks
at low temperatures is 30 seconds longer than that in summer. High thermal conductivity capsules reduce
the vulcanization time by 30 seconds compared to ordinary capsules. At the defoaming position, the
vulcanization time increases by 1 minute for every 1 mm increase in capsule thickness. The series connection
of high and low-pressure pipelines with the addition of a condensate drain tank can effectively reduce
condensed water in the pipeline, solving the consistent problem of insufficient vulcanization inside. The
average vulcanization time in the factory can be reduced by 30 seconds, resulting in a reduction of steam
consumption by 4,969 tons per year and a cost reduction of 1.39 million yuan.
Key words: tire blank temperature; thermal conductivity; vulcanization temperature; cost reduction and
efficiency improvement
(R-03)
·46· 第 51 卷 第 11 期

